After pretty bad oil usage and a compression check that showed 95psi for #4, it was time to rebuild the engine.
I wanted it done right so I towed it to Turbo Time in Cary, NC for the job. All rebuild pics courtesey of Turbo Time.
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Yep, there's our problem.
Looks like it screwed up the block too.
The bore was checked:
Pistons and rods were balanced:
Calico bearings were used as assembly began:
Pistons going in:
ARP studs secure the heads:
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